Lavaca River OperatingCompany

Myska #4ST

(API #: 42-157-32993)

Boling Salt Dome Prospect

Fort Bend County, Texas

Initial Completion Report

10-23-2014

Current operations: Move in Forbes rig

Total depth: 3830’MD Mud weight: N/A Viscosity: N/A Water loss: N/A

Activity: MIRU Forbes spot equipment. Fork lift racked pipe. NU BOP's. Tally pipe. RIH TO 3804 with bit & scraper. Lay down 10 joints. SDFN.

10-24-2014

Current operations: Perforate Well

Total depth: 3830’MD Mud weight: N/A Viscosity: N/A Water loss: N/A

Activity: POOH WITH TUBING BIT AND SCRAPER RU UNITED RIH WITH GR-N CCL TOOL AND RUN CBL. 98% CEMENT TO 3100. POOH PICK UP 5 ½ AS1X PACKER WITH WIRELINE REENTRY GUIDE 1 SLICK JOINT SEAT NIPPLE AND 111 JOINTS 2 3/8 TUBING SET PACKER AT 3529 WIYH 7500 LBS. COMPRESSION. TESTED BACKSIDE TO 500 PSI. ND BOPS NU TREE. RU UNITED RU LUBRICATOR RIH WITH LOGGING TOOLS AND 1 9/16 RTG 14 FT LOADED 6 SPF 60 DEGREE PHASING. RUN COORELATION LOG PERFORATE 3704-18. POOH RD UNITED. OPEN TO TANK NO SHOW RU SWAB LINE RIH TAG FLUID 25 FT. PULL 500 WELL ON VAC RIH TAG AT 150 PULL 600 WELL ON VAC RIH TAG 400 PULL 900 WELL ON VAC RIH TAG 850 PULL 1300 WELL ON VAC RIH TAG 1300 PULL 1800 WELL ON VAC RIH TAG 1800 PULL 2300 WELL ON VAC RIH TAG 2300 PULL 2800 ELL ON VAC. PUT WELL ON 10/64 CHOKE LEFT OPEN TO TANK.SDFWE.

10-27-2014

Current operations: Swabbing Well

Total depth: 3830’MD Mud weight: N/A Viscosity: N/A Water loss: N/A

Activity: Arrive location, no flow on well. RIH with swab, tag at 920’.Began swabbing, made 29 runs.Fluid feeding in at 75’ per minute, no oil cut in tank. Well on vac. Recovered 91 total since began swabbing, 75 bbl over capacity.

10-28-2014

Current operations: Swabbing Well/Plug Back

Total depth: 3830’MD Mud weight: N/A Viscosity: N/A Water loss: N/A

Activity: RIH with swab line tag at 420’. Made 16 runs recovered 47 additional bbls. ND Tree. NU BOP's POOH with tubing and packer. MIRU. United Surveys. RIH with CIBP. Set at 3690’ with 10’ cement on top. POOH. RD United. SDFN. Plan to re-perf tomorrow.

10-29-2014

Current operations: Plug back/Re-complete/swab well

Total depth: 3830’MD Mud weight: N/A Viscosity: N/A Water loss: N/A

Activity: RIH with tubing and packer.Set at 3517’.Test backside.ND BOP’s. NU tree.MIRUUnited Surveys. RIH with CCL logging tool and 1 9/16 RTG loaded 6 spf. Perforate 3565-83.POOH.RDMOUnited Surveys.RU swab line.Made 15 runs, recovered 29 bbls.Well on vacuum with little feed in.RD Forbes and release. Waiting on orders.

11-12-2014

Current operations: Plug back/Re-complete/swab well

Total depth: 3830’MD PBTD: 3680’ Mud weight: N/A Viscosity: N/A Water loss: N/A

Activity: MIRU United Surveys with mast truck. Hamman Swabbing on stand-by. RIH w/sinker bar, tagged fluid @2600’, fill @ 3650’ (30’ above cement plug). POOHUnited Surveys. RIH with CCL logging tool and 1 9/16 RTG loaded 6 spf. Perforate 3609-27’.POOH.RDMOUnited Surveys. 320# at surface. Installed 10/64” choke and run into tank. FTP down to 240# immediately, flowing small amount of gas and 3bbl of SW. FTP decreased to 50#, gas flow stopped and well began making oil in heads. Choke plugged up numerous times with gun junk. Made 3BO from 2-5PM with trace of water. Released Hamman from standby and left well into tank overnight on a 10/64”.